Loading...
Please wait, while we are loading the content...
Thrust performance of isolated 36-chute suppressor plug nozzles with and without ejectors at Mach numbers from 0 to 0.45
| Content Provider | Semantic Scholar |
|---|---|
| Author | Harrington, David E. Schloemer, J. J. Skebe, S. A. |
| Copyright Year | 1975 |
| Abstract | Plug nozzles with chute-type noise suppressors were tested with and without ejector shrouds at free-stream Mach numbers from 0 to 0.45 and over a range of nozzle pressure ratios from 2 to 4. A 36-chute suppressor nozzle with an ejector had an efficiency of 94.6 percent at an assumed takeoff pressure ratio of 3.0 and a Mach number of 0.36. This represents only a 3.4 percent performance penalty when compared with the 98 percent efficiency obtained with a previously tested unsuppressed plug nozzle. |
| File Format | PDF HTM / HTML |
| Alternate Webpage(s) | https://ntrs.nasa.gov/archive/nasa/casi.ntrs.nasa.gov/19760003038.pdf |
| Language | English |
| Access Restriction | Open |
| Content Type | Text |
| Resource Type | Article |