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Forward swept compressor testing
| Content Provider | NASA Technical Reports Server (NTRS) |
|---|---|
| Author | Miller, David P. |
| Copyright Year | 1997 |
| Description | A new forward-swept rotor designed by Allison Engine Company was tested in NASA Lewis Research Center's CE-18 facility. This testing was a follow-on project sponsored by NASA Lewis to study range enhancements in small turbomachinery. The test was conducted against a baseline rotor design that was also tested in CE-18. The design point for the rotor was a rotor pressure ratio of 2.69, a mass flow of 10.52 lbm/sec, and an adiabatic efficiency of 89.1 percent. Test data indicate that the rotor met the pressure ratio of 2.69 with a 10.77 lbm/sec flow rate, a 87.5-percent adiabatic efficiency, and a 19.5-percent stall margin. The baseline rotor achieved a pressure ratio of 2.69 at a 10.77 lbm/sec flow rate with a stall margin of only 9.2 percent and an adiabatic efficiency of 87.0 percent. The major differences are the significant stall margin increase and the substantially higher off-design peak efficiencies of the forward-swept rotor. The substantially higher performance over the baseline rotor design makes the new design a viable technology candidate for future products. |
| File Size | 51807 |
| Page Count | 2 |
| File Format | |
| Alternate Webpage(s) | http://archive.org/details/NASA_NTRS_Archive_20050179337 |
| Archival Resource Key | ark:/13960/t06x4923j |
| Language | English |
| Publisher Date | 1997-03-01 |
| Access Restriction | Open |
| Subject Keyword | Aircraft Propulsion And Power Augmentation Efficiency Rotors Pressure Ratio Turbomachinery Flow Velocity Compressors Mass Flow Ntrs Nasa Technical Reports ServerĀ (ntrs) Nasa Technical Reports Server Aerodynamics Aircraft Aerospace Engineering Aerospace Aeronautic Space Science |
| Content Type | Text |
| Resource Type | Technical Report |