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Experimental investigation of stage performance of j71 three-stage turbine
| Content Provider | NASA Technical Reports Server (NTRS) |
|---|---|
| Copyright Year | 1954 |
| Description | An experimental investigation of the stage performance of the J71 three-stage turbine at design speed and pressure ratio was conducted as part of a program involving research on the design and operational characteristics of high-work-output multistage axial-flow turbines. The investigation indicated that the over-all work output of the turbine based on temperature measurements at design speed and pressure ratio was 95 percent of the design value, with the greatest loss in work output and efficiency occurring in the first stage. Choking in the second-stage stator over most of the pressure ratios investigated prevented the attainment of design first-stage work output and also prevented any increase in work output of the first stage with increasing over-all pressure ratio at design speed. High losses in the first stage were a contributing factor to this choking condition. |
| File Size | 7886582 |
| Page Count | 19 |
| File Format | |
| Alternate Webpage(s) | http://archive.org/details/NASA_NTRS_Archive_19930093971 |
| Archival Resource Key | ark:/13960/t7wm5p91p |
| Language | English |
| Publisher Date | 1954-12-20 |
| Access Restriction | Open |
| Subject Keyword | Ntrs Nasa Technical Reports Server (ntrs) Nasa Technical Reports Server Aerodynamics Aircraft Aerospace Engineering Aerospace Aeronautic Space Science |
| Content Type | Text |
| Resource Type | Technical Report |