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Flight motor set 360l003 (sts-29r)
| Content Provider | NASA Technical Reports Server (NTRS) |
|---|---|
| Author | Riehr, Glen A. |
| Copyright Year | 1989 |
| Description | The redesigned solid rocket motor (RSRM) flight set 360L003 was launched on March 13, 1989 as part of NASA space shuttle mission STS-29R. As was the case with flight sets 360L001 and 360L002 (STS-26R and STS-27R), both motors (360L003A and 360L003B) performed in an excellent manner. Evaluation of the ground environment instrumentation measurements verified thermal model analysis data and showed agreement with predicted environmental effects. The right-hand aft field joint primary heater failed during the countdown; the secondary heater was activated and performed as designed. All other field joint heaters and aft skirt thermal conditioning systems had no anomalies. Shuttle thermal imager infrared readings compared favorably with measured ground environment instrumentation data. No thermal launch commit criteria violations occurred at any time. Evaluation of the development flight instrumentation showed exceptional propulsion performance. All ballistic parameters closely matched the predicted values and were well within the required specification levels. Girth and biaxial strain gage measurements compared closely with corresponding gages on previous flight motors, static tests, and with preflight predictions. Adequate safety factors were verified. (Some ignition transient spiking was noted in a few girth gages; the spiking was determined not to be representative of actual case behavior, but an instrumentation phenomena.) The accelerometers again measured high vibration amplitude levels during the ignition transient and the reentry Max Q phases. Postflight inspection showed that all combustion gas was contained by the insulation in the field and case-to-nozzle joints. No anomalous insulation erosion patterns were found, and the seals that did directly contain motor pressure showed no heat effects, erosion, or blowby. All anomalies identified were a result of splashdown damage, with the exception of fretting in the case field joint interference (nonsealing) surfaces and a prelaunch field joint heater failure. The disposition of all anomalies and the complete results are reported. |
| File Size | 12581018 |
| Page Count | 327 |
| File Format | |
| Alternate Webpage(s) | http://archive.org/details/NASA_NTRS_Archive_19900000854 |
| Archival Resource Key | ark:/13960/t4sj6cr7m |
| Language | English |
| Publisher Date | 1989-07-01 |
| Access Restriction | Open |
| Subject Keyword | Spacecraft Propulsion And Power Dynamic Structural Analysis Flight Tests Performance Tests Spacecraft Performance Propulsion System Performance Postflight Analysis Postlaunch Reports Space Shuttle Missions Engine Tests Space Shuttle Boosters Ascent Propulsion Systems In-flight Monitoring Ballistics Space Shuttle Ascent Stage Ntrs Nasa Technical Reports ServerĀ (ntrs) Nasa Technical Reports Server Aerodynamics Aircraft Aerospace Engineering Aerospace Aeronautic Space Science |
| Content Type | Text |
| Resource Type | Technical Report |