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Pmr graphite engine duct development
| Content Provider | NASA Technical Reports Server (NTRS) |
|---|---|
| Author | Stotler, C. L. Yokel, S. A. |
| Copyright Year | 1989 |
| Description | The objective was to demonstrate the cost and weight advantages that could be obtained by utilizing the graphite/PMR15 material system to replace titanium in selected turbofan engine applications. The first component to be selected as a basis for evaluation was the outer bypass duct of the General Electric F404 engine. The operating environment of this duct was defined and then an extensive mechanical and physical property test program was conducted using material made by processing techniques which were also established by this program. Based on these properties, design concepts to fabricate a composite version of the duct were established and two complete ducts fabricated. One of these ducts was proof pressure tested and then run successfully on a factory test engine for over 1900 hours. The second duct was static tested to 210 percent design limit load without failure. An improved design was then developed which utilized integral composite end flanges. A complete duct was fabricated and successfully proof pressure tested. The net results of this effort showed that a composite version of the outer duct would be 14 percent lighter and 30 percent less expensive that the titanium duct. The other type of structure chosen for investigation was the F404 fan stator assembly, including the fan stator vanes. It was concluded that it was feasible to utilize composite materials for this type structure but that the requirements imposed by replacing an existing metal design resulted in an inefficient composite design. It was concluded that if composites were to be effectively used in this type structure, the design must be tailored for composite application from the outset. |
| File Size | 63156663 |
| Page Count | 163 |
| File Format | |
| Alternate Webpage(s) | http://archive.org/details/NASA_NTRS_Archive_19900000721 |
| Archival Resource Key | ark:/13960/t72v7fk8g |
| Language | English |
| Publisher Date | 1989-08-01 |
| Access Restriction | Open |
| Subject Keyword | Aircraft Propulsion And Power Fabrication Ducts Milling Cost Reduction Weight Reduction Graphite Turbofan Engines Cost Analysis Composite Structures Ntrs Nasa Technical Reports Server (ntrs) Nasa Technical Reports Server Aerodynamics Aircraft Aerospace Engineering Aerospace Aeronautic Space Science |
| Content Type | Text |
| Resource Type | Technical Report |