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Unsuccessful concepts for aircraft wake vortex minimization
| Content Provider | NASA Technical Reports Server (NTRS) |
|---|---|
| Author | Dunham Jr., R. E. |
| Copyright Year | 1977 |
| Description | Exploratory concepts are described which were investigated to achieve a reduction in the vortex induced rolling upsets produced by heavy aircraft trailing vortexes. The initial tests included the use of mass injection, oscillating devices, wingtip shape design, interacting multiple vortexes, and end plates. Although later refinements of some of these concepts were successful, initial test results did not indicate a capability of these concepts to significantly alter the vortex induced rolling upset on a following aircraft. |
| File Size | 2424974 |
| Page Count | 29 |
| File Format | |
| Alternate Webpage(s) | http://archive.org/details/NASA_NTRS_Archive_19780004080 |
| Archival Resource Key | ark:/13960/t3c01052m |
| Language | English |
| Publisher Date | 1977-01-01 |
| Access Restriction | Open |
| Subject Keyword | Aerodynamics Flight Tests Vortices Aircraft Wakes Wing Tips Vortex Breakdown Aircraft Design End Plates Rolling Moments Ntrs Nasa Technical Reports ServerĀ (ntrs) Nasa Technical Reports Server Aircraft Aerospace Engineering Aerospace Aeronautic Space Science |
| Content Type | Text |
| Resource Type | Article |