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Performance of the csm rcs during the as 506/csm 107/lm 5 mission (apollo 11)
| Content Provider | NASA Technical Reports Server (NTRS) |
|---|---|
| Copyright Year | 1969 |
| Description | The Apollo 11 service module and the command module (CM) reaction control system performed satisfactorily throughout the mission. Two anomalies which occurred were an inadvertent isolation valve closure during command and service module/Saturn S4B/lunar module separation and a failure of a CM thruster to respond to automatic commands. The isolation valves were later opened by the crew and remained open during the remainder of the mission. The cause of the closure was determined to be the shock loads generated during separation. The CM engine malfunction was caused by a faulty terminal board connector. All system parameters were normal during the mission, and all mission requirements were satisfied. |
| File Size | 3115281 |
| Page Count | 60 |
| File Format | |
| Alternate Webpage(s) | http://archive.org/details/NASA_NTRS_Archive_19720017210 |
| Archival Resource Key | ark:/13960/t8jd9mj3k |
| Language | English |
| Publisher Date | 1969-12-31 |
| Access Restriction | Open |
| Subject Keyword | Space Sciences Ntrs Nasa Technical Reports ServerĀ (ntrs) Nasa Technical Reports Server Aerodynamics Aircraft Aerospace Engineering Aerospace Aeronautic Space Science |
| Content Type | Text |
| Resource Type | Technical Report |